DHtimeline_summary
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Sources Legend:
Schlumberger Timeline
BP
Transocean
USCG (20 Anomalies)
Other
Date
Mar-08
Feb-09
4/4/2009
6/22/2009
9/29/2009
10/7/2009
10/07/2009 -10/31/2009
10/31/2009 -11/2/2009
11/8/2009
11/26/2009
2/9/2010
3/8/2010
3/10/2010
3/10/2010
03/10/2010 - 03/12/2010
3/13/2010
4/1/2010
4/5/2010
4/6/2010
4/6/2010
4/6/2010
4/8/2010
4/9/2010
4/9/2010-4/15/2010
4/10/2010
4/10/2010
4/14/2010
4/15/2010
4/15/2010
4/15/2010
4/16/2010 [14:00]
4/17/2010
4/17/2010 [12:00]
4/18/2010 [00:30]
4/18/2010
4/18/2010-4/19/2010
4/19/2010 [13:30-17:30]
4/19/2010 [17:30-19:30]
4/19/2010 [17:30]
4/19/2010
4/20/2010
4/20/2010 [00:30]
4/20/2010 [03:00-04:00]
4/20/2010 [07:00]
4/20/2010 [7:00]
4/20/2010 [11:15]
4/20/2010 [12:00]
4/20/2010 [12:00]
4/20/2010 [14:15-17:30]
4/20/2010 [15:00]
4/20/2010 [15:54]
4/20/2010 [15:56]
4/20/2010 [15:56-16:53]
4/20/2010 [16:00-16:15]
4/20/2010 [16:28]
4/20/2010 [16:29]
4/20/2010 [16:52]
4/20/2010 [16:53-16:55]
4/20/2010 [16:55-16:57]
4/20/2010 [16:54-16:58]
4/20/2010 [16:58]
4/20/2010 [16:57]
4/20/2010 [17:00]
4/20/2010 [17:05]
4/20/2010 [17:05]
4/20/2010 [17:05-17:25]
4/20/2010 [17:15]
4/20/2010 [17:25]
4/20/2010 [17:27]
4/20/2010 [17:27-17:52]
4/20/2010 [17:52]
4/20/2010 [17:52]
4/20/2010 [17:52-18:40]
4/20/2010 [18:00-19:00]
4/20/2010 [18:10-20:10]
4/20/2010 [18:40]
4/20/2010 [18:40]
4/20/2010 [18:45-19:12]
4/20/2010 [19:12-19:48]
4/20/2010 [19:55]
4/20/2010 [19:55]
4/20/2010 [20:00-21:08]
4/20/2010 [20:35-21:05]
4/20/2010 [20:30-20:45]
4/20/2010 [20:58]
4/20/2010 [21:00-21:10]
4/20/2010 [21:08]
4/20/2010 [21:08-21:14]
4/20/2010 [21:10]
4/20/2010 [21:14]
4/20/2010 [21:31]
4/20/2010 [21:31-21:36]
4/20/2010 [21:45]
4/22/2010
Description of Events
BP purchases the mineral rights to drill for oil at the Macondo well at the Minerals
Management Service's (MMS) Lease Sale #206, held in New Orleans. The well is
located in Mississippi Canyon Block 252 in the United States sector of the Gulf of
Mexico approx. 41 miles (66 km) off the Louisiana coast.
BP files a 52 page exploration and environmental impact plan for the Macondo well with the MMS. The
plan stated that it was "unlikely that an accidental surface or subsurface oil spill would occur from the
proposed activities".38 In the event an accident did take place the plan stated that due to the well being
48 miles (77 km) from shore and the response capabilities that would be implemented, no significant
The Department of the be expected.
adverse impacts would Interior exempted BP's Gulf of Mexico drilling operation from a detailed
environmental impact study after concluding the unlikelihood of a massive oil spill.
Mark E. Hafle, a senior drilling engineer at BP, warns of the likelihood of collapse of the metal casing for
the blowout preventer under high pressure.
Schlumberger crew arrives on Transocean Marianas to perform logging, measuring, and drilling services
for BP on Mississippi Canyon Block 252 ("MC252") . Specifically, BP, contracted with Schlumberger to
perform logging while drilling, measuring while drilling, and directional drilling services.
The Transocean Marianas semi-submersible rig begins drilling of the Macondo well.
Schlumberger crew performs logging, measuring, and drilling services for BP.
Schlumberger crew departs Transocean Marianas in advance of approaching Hurricane Ida.
Transocean Marianas sustains damage in Hurricane Ida.
Transocean tows Transocean Marianas to shipyard for repairs. Transocean Marianas does not return to
MC252.
Transocean Deepwater Horizon commences activities in MC252. BP contracted with Halliburton to
perform logging while drilling, measuring while drilling, directional drilling services and cementing on
the Transocean Deepwater Horizon. BP contracted with Schlumberger tOPJ ovide wireline oQen and
cased hole services.
Target date for the completion of the well which had been budgeted to cost $96 million
Well flowed at 13,305 feet. Lost circulation. Stuck drill pipe
Schlumberger crew arrives on Transocean Deepwater Horizon to perform a wireline cased hole service
for BP. Specifically, the drilling pipe in the weUbore stuck during drilling. BP requests Schlumberger to
try to determine where the drilling pipe was stuck in the well bore so the drilling pipe above that point
could be removed. performs wireline cased hole logging service to identify free drilling pipe for pipe
Schlumberger crew
retrieval. During the performance of this service, the tool used by Schlumberger becomes lodged and is
abandoned. BP reimburses Schlumberger for the cost of the tool.
Schlumberger crew deports Transocean Deepwater Horizon.
Marvin Volek, a Halliburton employee, warns that BP's use of cement "was against our best practices"
Schlumberger crew orrives on Transocean Deepwater Horizon to perform wireline open hole logging and
testing services for BP. BP informs Schlumberger crew that drilling activities not yet completed and
sends crew home.
MMS issues permit to BP for the well, noting: "Exercise caution while drilling due to indications of
shallow gas and possible water flow."
Schlumberger crew deports Transocean Deepwater Horizon.
Witness stated pieces of rubber returned in mud flow over shakers
Estimated to be from stripping operations during well control event (~1300 ft pipe stripped) Expected
normal wear on lower annular rubber element
Schlumberger crew returns to Transocean Deepwater Horizon to perform wireline open hole logging and
testing services for BP. Specifically, BP contracted with Schlumberger to perform an evaluation of the
formation characteristics for porosity and permeability, and to gather fluid pressures and samples.
BP drills last section with the wellbore 18,360 feet (5,600 m) below sea level but the last 1,192 feet (363
m) needs casing. BP chooses to do a single liner with fewer barriers that is faster to install and cheaper
($7 to $10 million) against Halliburton‟s recommendation of using a liner/ tieback casing that will
provide redundant barriers to flow.
Finish Drilling
9-7/8"x8-1/2" Open Hole
14.0 ppg mud inside and out
Trip out with drilling
Wireline log for 4 days
Annular passed subsequent pressure test on 10 April (250psi/3500psi)
Schlumberger crew performs wireline open hole logging and testing services for BP.
BP drilling engineer Brian Morel, emails a colleague "this has been [a] nightmare well which has
everyone all over the place."
Bp Drilling engineer Brian Morel informs Jesse Gagliano,a Halliburton executive, that they plan to use 6
centralizers for the casing. Gagliano‟s modeling showed that it would require 21 centralizers to achieve
only “MINOR” gas flow problem. Morel„s response in his email was "it's too late to get any more product
on the rig, our only option is to rearrange placement of these centralizers." Gagliano also recommends to
circulate the drilling mud from the bottom of the well all the way up to the surface to remove air pockets
and debris which can contaminate the cement, saying in an email, "at least circulate one bottoms up on
the well before doing a cement job." Despite this recommendation, BP cycles only 261 barrels (41.5 m3)
BP chose fraction a the total mud used in instead
of mud, a to installof single string of casingthe well.of a linear and tieback, applying for an amended
permit on April 15. MMS approves amended permit for BP to use a single liner with fewer barriers on
the same day. crew deports Transocean Deepwater Horizon.
Schlumberger
Run in hole for wiper trip
Circulate bottoms up at TD
Pump high vis sweep
Monitor for gains or losses-none
14.0 ppg mud throughout before trip out
Pump out from 18360'-14759'
Deepwater Horizon completes its drilling and the well is being prepared to be cemented so that another
rig will retrieve the oil. The blowout preventer is tested and found to be "functional." Gagliano now
reports that using only 6 centralizers "would likely produce channeling and a failure of the cement job."
4 flow checks during trip out-no flow
Make trip tp retreive wear sleeve
Retreval successful
Run 7"x9-7/8" production casing
Crossover at 12487
Float collar at 18114'
Shoe at 18304'
56' of rat hole
Laid out three joints of 7" due to damaged threads
Saw 10K weight bobble at 18218
9 attemps to convert float equipment
Gagliano's report says "well is considered to have a severe gas flow problem."
Schlumberger wireline cased hole crew arrives on Transocean Deepwater Horizon. Specifically, BP
contracted with Schlumberger to be available to perform a cement bond log and set a bridge plug and/or
cement retainer, should BP request those services.
Had to pressure up on the cement shoe valves nine times to convert from “filling the casing” to act as a
check valve, per BP morning report
Low pump pressures. Return flow after float shear out appeared to be high
Sheared at 3142 psi vs 500-700 psi design
Circulate 342 bbl before cement job
Pump nitrified foam cement
Estimated TOC at 17260'
Bumped plug with 1150 psi
Cement in place at 00:35
Bled back 5 bbls to 0 psi
Minimal calculated U-tube pressure after (nearly balanced)
Minimal U-tube may have prevented definitive float test
14 ppg mud in rathole with 16.7 ppg cement in shoe track
Halliburton completes cementing of the final production casing string.
BP officials gather on the platform to celebrate seven years without an injury on the rig.
Potential for contamination of cement in shoe track due to density difference between cement and mud
Release running tool
Set seal assembly at 5059' to seal the 9-7/8" casing annulus
Successful pressure test of seal assembly
Setting and testing procedure as per plan
Running string for the 9-7/8 X 7 inch casing pulled wet after the seal assembly test was completed.
Running string pulled three stands wet and so they slugged the wellbore with a 30 bbls - 16.3 ppg pill
Begin tripping out
Run in with tapered string for cement plug
6-5/8"x5-1/2"x3-1/2" drill pipe
Stop at 4700' (above BOP)
Close blind shear rams
At approximately 7:00 a.m., BP informs Schlumberger crew that no wireline cased hole services will be
requested and BP sends Schlumberger crew home.
At approximately 11 :15 a.m., Schlumberger crew departs Transocean Deepwater Horizon on regulorly
scheduled BP helicopter flight.
Positive test casing to 250 and 2500 psi
Finish RIH to 8367'
15 bbl gain in the trip tank after the casing test pressure was released, this seem a little large for pressure
bleed back for fluid compression and would expect 5 bbl gain.
Hard to track fluid volumes in the wellbore when you are pumping mud to boat (if from pits) and also
pump saltwater into the hole (from sea chest)
Mud transfer to boat begins at 13:28
Displaced booster line w/ seawater
Displaced choke line with seawater
Displaced kill line with seawater
1200 psi trapped in kill line
Pump 454 bbls LCM spacer (16.0 ppg)
Form-a-Set + Form-a-Squeeze combination
Viscous, solids-laden fluid
High u-tube pressure on DP of 2324 psi. Calculated u-tube should be 1628 psi.
Flow out exceeds flow in indicating the well is possibly flowing (per electronic data). Note the electronic
data shows increased gas units during this time period.
Kill line pressure holds at 1200 psi
Pump 352 bbls seawater
Not enough to get spacer above BOP
2325 psi static pressure after pumping
Calculated U-tube is 1628 psi
Shut annular
Bleed drill pipe pressure from 2325 psi to 1220 psi to equalize with kill line
High bleed back volume. Suspect the Annular Preventer is leaking at this point. Discovery Wells data
shows mud being transferred into the trip tank from the mud pits and 50 barrels of mud coming out of the
trip tank. Both Kaluza and Lambert statements confirm the rise was topped up at this time. Lambert
statement also indicates that the Annular was leaking. BP Trainee WSL (Lambert) on floor. First time
well temporarily underbalance when bled to 251 on the DP. First time well temporarily underbalance
when bled to 251 on the DP.
Pressure building drill pipe.
Open kill line
Pressure equalizes
Drillpipe pressure goes to 1400 psi
Kill line pressure drops to 645 psi
Bleed pressure to 273 psi on drillpipe as kill line pressure drops to zero
DP pressure never gets to zero
First time well is under balance
Observed that fluid level in the riser had dropped
Set up for negative pressure test began
Suspect the annular is leaking
Shut in drillpipe
Pressurer builds to 1250 psi in 6 minutes
Filled the riser with 50 bbls from trip tank
Mud offload to Bankston ends at 17:17
Performed first negative test down the workstring, had 1250 psi on the work sting. Some employees
recalled a disagreement between Transocean and BP on the rig floor about the negative test and pressure
on the work string.
60 barrels of spacer moved below annular
Increased annular activating pressure from 1200 to 1900 psi
Set up fluids through crew handover at 18:00
Under-displaced 16 ppg spacer
Spacer was not in MMS permit
Position under annular led to confusing pressure reading
Float equipment under tested by 285 psi
Mudloggers not informed that offloading had ceased
Bleed drillpipe from 1202 to 0 psi
An additional 15 bbls of fluid bled from DP.
IBOP is then closed
Pressure monitored through cement unit quickly rises to 790 psi and falls
Fluid bled from kill line and continues to flow. Opened kill line to Halliburton cement unit, had 700 psi
and bled 3 to 15 bbls. Flow did not stop and spurting could be indication of kill line plugging. Flow shut
in at cement unit at approximately 1759.
About fluid volumes due to movement below annular and line up for monitoring –either from drill pipe
(normal procedure used by rig) or kill line (MMS permit)
Either line up is appropriate and will correctly monitor well
Took about two hours for the company man to confirm a good second negative test due to 1400 psi on
the cement pump / displacement string.
Pressure slowly builds from 0 to 1400 psi over 31 minutes
Drillpipe pressure (monitored at Haliburton) stays steady at 1400 psi
Pumped on kill line to ensure full
Bled off 0.2 bbla to trip tank
Monitored kill line for 30 minutes
DP pressure builds to 1400 psi Kaluza and Vidrine arrive at rig floor together at approx.1910. Discussion
again about DP pressure anomaly. Apparently explained by TO personnel as 'bladder effect' or 'annular
compression'.
DP pressure stable at 1400 psi and no flow from kill line.
Prepare to displace with seawater
Pumped 1304 bbl seawater
Using rig pumps and booster
Shut down for sheen test - spacer back
1017 psi on DP when shut down
Sheen test passes
Mud circulation out prior to second plug –well reaches highest underbalanced pressure to this point.
Electronic data shows pit gain of approx. 40 bbls.
Flow out exceeds flow in indicating the well is possibly flowing (per electronic data).
Trip tank being discharged to pits through flow line (normal procedures ahead of change from oil to
water mud in active system) Start dumping of Trip Tank to flow line; Driller expects to see flow increase
(Gain 15.4 bbls)
At same point pumps ramp down for stop at static sheen test
Increased flow out due to discharge of trip tank
Driller expected to see flow increase
Flow returned near pre-tank discharge level when trip tank pump stopped, THEN increased
Potentially masked the gain
Flow out exceeds flow in indicating the well is possibly flowing (per electronic data).
Shut down for static sheen test to begin going over board with water-based spacer.
Pressure on drill pipe when shut down and flow from well. DP pressure increased from 1000 psi to 1250
psi during sheen test.
Sperry Sun sensors failure to record a flow out after 21:1021
Crew instructed to divert to divert returns overboard
Pumping stopped. Problem observed by rig floor and pumping is stopped. Possibly report from mud pit
room that mud returning and being sent overboard. Had pumped 265 bbls since sheen test.
Time taken to get well shut in.
Gas, oil and concrete from the Deepwater Horizon explode up the wellbore onto the deck and then
catches fire. One hundred twentysix people were on the Deepwater Horizon drilling rig when the incident
occurred. 11 remain unaccounted for; 17 were injured, 3 of them critically.
The Deepwater Horizon drilling unit sinks
Date
2004
1
4/15/2010
2
4/15/2010
3
4/16/2010
4
4/20/2010
5
4/20/2010 (?)
6
7 4/20/2010 [15:00]
8 4/20/1010 [15:56]
9 4/20/2010 [17:00 - 20:10]
10
11
12
13
14
15
16
17
18
19
20
21
22
23
24
4/20/2010
25
26
27
28
29
Risk Based Decision
Variable Bore Ram changed to Test Ram – acknowledged risk conversion will reduce built in redundancy
Centralizers – Halliburton proposed 21, BP went with 6.
Well Design –
a. Long string vs. tieback (provides additional barriers)
b. 7” from Nexen at last minute
c. Change of connectors
Circulate Bottoms Up – gas cut mud w/ cement (channeling)
Circulated bottoms up only to the wellhead rather than to the surface
Cement Bond Log – Schlumberger personnel on rig to run CBL and set bridge plug with equipment (4/18-4/20)
Schlumberger sent home due to interpretation of cement “analysis”
Not to run the OD lock ring and/or lock down sleeve – timing w/in procedure - BP elected to defer installation
of the lockdown sleeve until after the well had been displaced with seawater
Pumping mud to boat while displacing riser – unable to accurately monitor volume in-out
LCM Spacer – pumped 450 bbl LCM as spacer across BOP/choke-kill lines
Negative test interpretation and proceeding forward – lack of define procedure and successful test
Timing of setting the surface plug
Cement designed for balanced not overbalanced
Deviating from own recommended practices – API RP 65
Continuing operations w/BOP leaks and yellow pod functions being locked out
Cut back on cement to have enough room to run CBL
Decision to forgo drilling survey /ABS since 2005
Utilization of nitrogen foamed cement at this depth - use of Foam Cement a Poor Choice?
- May be uncommon at this depth
- Typically used for shallow conductor casing string
Did the operator give the cement enough time to cure? (from Halliburton lab test reports)
- Test on 3/29 of 9-7/8”liner slurry (previous casing): 15 hours needed to reach 2100 psi compressive strength
- Test on 4/12 of 7”casing slurry : 0 psi compressive strength after 24 hours; needed 48 hours to reach
compressive strength of 1590 psi
o Negative test started ~18 hours after pumped
Was the volume for 7”production casing cement job appropriate?
- 60 bblspumped (requested third party caliper logs to determine if adequate)
- 16.7 ppgcement in shoe track over 14 ppgmud in open hole beneath the 7”shoe
o could fall out into the open hole
- Estimate of 2 bblsnitrogen cement in shoe track –normally would pump all into annulus
Wiper plug was run through two casing internal diameters
1st positive test on casing against wiper plug at 10 hours set time
Was outer lock ring run on assembly?
- Need to understand rating or tolerance for pressure on annulus side
Running production casing that was pre-doped shoreside & probably no inspection on rig floor.
Positive pressure tests on cement and casing too low.
Circulated out riser with no pit level monitoring at any point.
Ignored pvt indications of excess flow while circulating out riser first hour and 10 minutes-to 21:10 hours 4-20-
10.
Bypassed pvt flow-out indicator after 21:10 by putting returns directly overboard.
Ignored drill pipe pressure with pump off at 21:20 and 21:30 with seawater most all the way around.
Not watching for riser flow with pump off at those times or not responding to an apparent flow
Not closing bop and diverter at 21:20 to monitor pressures and divert flow overboard.
Outcome
Failure to Activate BOP
Due to model
i. <10 suggested
“moderate gas possible”
ii. 6 suggested “SEVERE”
Insufficient barriers
Potential cuttings in well
bore
- Potential non-
homogeneous mud or
gas content
o Could lead to cement
channeling and flow path
for formation fluids
Potential for mud
bypassing plug into
cement
potential to slightly open
flappers during cure time
Time Breakdown of Drilling Activities (Taken From Transocean Daily Drilli
Date
3/26/2010
TIME LOG
ELAPSED TIME CODE NO.
FROM TO
00:00 00:30 0H30M 12
00:30 01:00 0H30M 12
01:00 02:00 1H0M 5
02:00 02:30 0H30M 5
02:30 06:30 4H0M 6
06:30 07:00 0H30M 6
07:00 07:30 0H30M 6
07:30 08:00 0H30M 6
08:00 09:30 1H30M 6
09:30 11:00 1H30M 6
11:00 12:00 1H0M 6
TIME LOG
ELAPSED TIME CODE NO.
FROM TO
12:00 12:30 0H30M 6
12:30 13:30 1H0M 6
13:30 14:00 0H30M 5
14:00 14:30 0H30M 9
14:30 15:30 1H0M 9
15:30 16:30 1H0M 15
16:30 18:30 2H0M 6
18:30 19:30 1H0M 6
19:30 22:00 2H30M 6
22:00 23:00 1H0M 15
23:00 00:00 1H0M 15
3/27/2010
TIME LOG
ELAPSED TIME CODE NO.
FROM TO
00:00 03:30 3H30M 15
03:30 04:00 0H30M 1
04:00 04:30 0H30M 6
04:30 08:00 3H30M 15
08:00 08:30 0H30M 15
08:30 09:00 0H30M 6
09:00 12:00 3H0M 3
TIME LOG
ELAPSED TIME CODE NO.
FROM TO
12:00 16:00 4H0M 3
16:00 16:30 0H30M 5
16:30 17:30 1H0M 5
17:30 18:00 0H30M 5
18:00 20:00 2H0M 3
20:00 20:30 0H30M 2
20:30 21:00 0H30M 5
21:00 21:30 0H30M 6
21:30 22:30 1H0M 6
22:30 23:00 0H30M 6
Depth Mudweight
15043 13.4
4/3/2010
TIME LOG
ELAPSED TIME CODE NO.
FROM TO
00:00 01:30 1H30M 2
01:30 02:00 0H30M 2
02:00 08:30 6H30M 2
08:30 09:30 1H0M 5
09:30 11:00 1H30M 2
11:00 12:00 1H0M 3
TIME LOG
ELAPSED TIME CODE NO.
FROM TO
12:00 13:30 1H30M 3
13:30 16:30 3H0M 5
16:30 17:00 0H30M 3
17:00 20:00 3H0M 5
20:00 21:00 1H0M 2
21:00 21:30 0H30M 15
21:30 22:30 1H0M 3
22:30 00:00 1H30M 2
Depth Mudweight
17676 14.3
4/9/2010
TIME LOG
ELAPSED TIME CODE NO.
FROM TO
00:00 02:30 2H30M 3
02:30 03:30 1H0M 5
03:30 06:30 3H0M 5
06:30 07:00 0H30M 3
07:00 08:30 1H30M 5
08:30 12:00 3H30M 2
Depth Mudweight
18260 14
TIME LOG
ELAPSED TIME CODE NO.
FROM TO
12:00 12:30 0H30M 2
12:30 19:00 6H30M 5
19:00 21:30 2H30M 6
21:30 22:00 0H30M 6
22:00 23:00 1H0M 15
23:00 00:00 1H0M 15
4/10/2010
TIME LOG
ELAPSED TIME CODE NO.
FROM TO
00:00 03:30 3H30M 15
03:30 04:00 0H30M 15
04:00 04:30 0H30M 6
04:30 05:00 0H30M 5
05:00 08:30 3H30M 15
08:30 09:00 0H30M 15
09:00 12:00 3H0M 6
TIME LOG
ELAPSED TIME CODE NO.
FROM TO
12:00 13:00 1H0M 6
13:00 13:30 0H30M 5
13:30 18:30 5H0M 6
18:30 19:30 1H0M 6
19:30 20:00 0H30M 6
20:00 20:30 0H30M 6
20:30 21:00 0H30M 6
21:00 23:00 2H0M 11
23:00 00:00 1H0M 11
4/17/2010
TIME LOG
ELAPSED TIME CODE NO.
FROM TO
00:00 00:30 0H30M 6
00:30 01:00 0H30M 6
01:00 01:30 0H30M 15
01:30 02:00 0H30M 5
02:00 06:00 4H0M 6
06:00 06:30 0H30M 6
06:30 08:30 2H0M 6
08:30 09:30 1H0M 6
09:30 10:00 0H30M 6
10:00 11:00 1H0M 6
11:00 11:30 0H30M 6
11:30 12:00 0H30M 6
TIME LOG
ELAPSED TIME CODE NO.
FROM TO
12:00 12:30 0H30M 6
12:30 13:00 0H30M 6
13:00 13:30 0H30M 6
13:30 16:00 2H30M 6
16:00 16:30 0H30M 3
16:30 17:00 0H30M 6
17:00 18:00 1H0M 6
18:00 19:00 1H0M 6
19:00 19:30 0H30M 3
19:30 22:00 2H30M 6
22:00 22:30 0H30M 6
22:30 23:00 0H30M 6
23:00 23:30 0H30M 6
23:30 00:00 0H30M 6
4/20/2010
TIME LOG
ELAPSED TIME CODE NO.
FROM TO
00:00 00:30 0H30M 12
00:30 01:00 0H30M 12
01:00 02:00 1H0M 12
02:00 02:30 0H30M 12
02:30 03:00 0H30M 12
03:00 03:30 0H30M 12
03:30 04:00 0H30M 12
04:00 05:00 1H0M 5
05:00 06:30 1H30M 12
06:30 07:00 0H30M 12
07:00 07:30 0H30M 12
07:30 08:00 0H30M 6
TIME LOG
ELAPSED TIME CODE NO.
FROM TO
12:00 12:30 0H30M 6
12:30 13:30 1H0M 6
13:30 14:00 0H30M 12
14:00 14:30 0H30M 15
14:30 15:00 0H30M 5
down of Drilling Activities (Taken From Transocean Daily Drilling Reports)
(Based on Available Daily Drilling Reports)
DETAILS OF OPERATIONS IN SEQUENCE AND REMARKS
(M) (On) PERFORM EXPANSION PROCEDURE TO SET CASIND HANGER PER HALLIBURTON WITH 5,000 PSI. MONITOR WELL ON
TRIP TANK
(M) (On) RIG DOWN CEMENT HEAD AND LAID DOWN ON RISER SKATE. MONITOR WELL ON TRIP TANK.
(M) (On) DROP NERF BALL AND PUMP 2 STRING VOLUMES. MONITOR ACTIVE SYSTEM FOR GAINS OR LOSSES.
(M) (On) PUMP 50 BBLS OF 15 PPG SLUG. MONITOR ACTIVE SYSTEM FOR GAINS OR LOSSES.
(M) (On) PULL OUT OF HOLE FROM 12,817' TO 45'. MONITOR DISPLACEMENT ON TRIP TANK.
(M) (On) LAY DOWN CASING HANGER RUNNING TOOL FROM 45' TO SURFACE. MONITOR DISPLACEMENT ON TRIP TANK.
(M) (On) CLEAN AND CLEAR RIG FLOOR AND RIG DOWN CASING HANDLING TOOL FROM FWD PRS. MONITOR WELL ON TRIP
TANK.
(M) (On) HELD PER-JOB SAFETY MEETING ON PICKING UP 10 5/8" X 12 1/4" DRILLING ASSEMBLY. MONITOR WELL ON TRIP TANK.
(M) (On) PICK UP 10 5/8" X 12 1/4" DRILLING ASSEMBLY FROM RISER SKATE. FROM SURFACE TO 130' MONITOR DISPLACEMENT
ON TRIP TANK
(M) (On) PROGRAM MWD TOOLS. MONITOR WELL ON TRIP TANK.
(M) (On) CONTINUE PICKING UP 10 5/8" X 12 1/4" DRILLING ASSEMBLY FROM 130' TO 450'. MONITOR DISPLACEMENT ON TRIP
TANK
DETAILS OF OPERATIONS IN SEQUENCE AND REMARKS
(M) (On) HOLD PRE-JOB MEETING WITH CREW ON TRIPPING IN HOLE. MONITOR WELL ON TRIP TANK.
(M) (On) TRIP IN HOLE FROM 450' TO 4028'. CHANGE OUT JARS GOING IN THE HOLE. MONITOR PIPE DISPLACEMENT ON TRIP
TANK
(M) (On) FILL DRILL PIPE. SHALLOW TEST MWD TOOLS. MONITOR ACTIVE FOR GAINS OR LOSSES.
(M) (On) HOLD PRE-JOB MEETING ON SLIPPING DRILL LINE. MONITOR WELL ON TRIP TANK.
(M) (On) SLIP 100' OF DRILL LINE. MONITOR WELL ON TRIP TANK. RESET FLOOR SAVER AND RECALIBRATE BLOCK. VERIFY
CROWN SAVER. WHILE SLIPPING DRILL LINE BEGIN CASING TEST TO 1800 PSI HIGH.
(M) (On) CONTINUE WITH CASING TEST WITH 1800 PSI FOR 30 MINUTES. TEST BLIND SHEAR RAMS FROM TOOLPUSHER'S CONTROL (M) (On) CONTINUE
WITH CASING TEST WITH 1800 PSI FOR 30 MINUTES. TEST BLIND SHEAR RAMS FROM TOOLPUSHER'S CONTROL PANEL ON YELLOW POD TO 250 PSI LOW
AND 1800 PSI HIGH FOR 5 MINUTES EACH TEST. SEE TEST CHARTS FOR ADDITIONAL INFORM FUNCTION TEST BLIND SHEAR RAMS FROM DRILLER'S
CONTROL PANEL ON BLUE POD AT 16:22 HRS. MONITOR RISER ON TRIP TANK.
(M) (On) TRIP IN HOLE FROM 4,028' TO 9,259' MONITOR PIPE DISPLACEMENT ON TRIP TANK. WHILE TRIPPING HOLE, TEST CHOKE MANIFOLD TO 250 PSI
LOW AND 6500 PSI HIGH, TEST ALL BUFFER VALVES TO 250 PSI LOW AND 5000 PSI HIGH FOR 5 MINUTES EACH TEST OR GREEN LIGHT ON DIGITAL
ANATOMIZED BOP TEST.
(M) (On) PICKUP 3 STANDS OF 5 1/2" TEST PIPE MAKING UP EACH JOINT BREAKING OUT INPECTING THREADS, REDOPING
THREADS AND MAKING UP. MONITOR PIPE DISPLACEMENT ON TRIP TANK.
(M) (On) TRIP IN HOLE FROM 9,552' TO 14.503'. MONITOR PIPE DISPLACEMENT ON TRIP TANK.
(M) (On) FILL DRILL PIPE. PICKUP TEST KELLY LOCATE ON UPPER ANNULAR TO VERIFY 5 1/2" RANGE 2 DRILL PIPE ACROSS
BOP'S. RIG UP CHICKSAN LINES. MONITOR PIPE DISPLACEMENT ON TRIP TANK.
(M) (On) RIG UP CHICKSAN LINES. TEST LINES TO 8000 PSI. MONITOR WELL ON TRIP TANK.
DETAILS OF OPERATIONS IN SEQUENCE AND REMARKS
(M) (On) TEST SUB SEA BOP'S AS PER BP AND MMS REQUIREMENTS ON 5 1/2" DRILL PIPE TEST PREFORMED FROM TOOL PUSHERS CONTROL PANEL ON
YELLOW POD. TEST UPPER ANNULAR AND KELLY HOSE TO 250 PSI LOW AND 5,000 PSI HIGH. TEST LOWER ANNUL TO 250 PSI LOW AND 3,500 PSI HIGH.
TEST ALL PIPE RAMS AND FAILSAFE VALVES TO 250 PSI LOW TO 6,500 PSI HIGH . TEST PREFORMED USING HALLIBURTONS AUTOMATIZED TEST
PROCEDURE. SEE TEST CHARTS FOR ADDITIONAL INFORMATION.
(M) (On) RIG DOWN CHICKSAN LINES AND SURFACE TESTING EQUIPMENT. LAY OUT TEST KELLY ON RISER SKATE.
(M) (On) RUN IN HOLE FROM 14,503' TO 14,778'. MONTIOR PIPE DISPLACEMENT ON TRIP TANK.
(M) (On) TEST SUB SEA BOP'S AS PER BP AND MMS REQUIREMENTS ON 6 5/8" DRILL PIPE TEST PREFORMED FROM TOOL PUSHERS CONTROL PANEL ON
YELLOW POD. TEST UPPER ANNULAR AND LOWER ANNULAR TO 250 PSI LOW AND 3,500 PSI HIGH. TEST ALL PIPE RAMS AND FAILSAFE VALVES TO 250 PSI
LOW TO 6,500 PSI HIGH . TEST PREFORMED USING HALLIBURTONS AUTOMATIZED TEST PROC SEE TEST CHARTS FOR ADDITIONAL INFORMATION.
(M) (On) FUNCTION TEST SUB SEA BOP'S FROM DRILLERS CONTROL PANEL ON BLUE POD. DIVERTER FUNCTIONED AT 08:00
HRS.
(M) (On) RUN IN HOLE FROM 14,778' TO 14,906'. MONITOR PIPE DISPLACEMENT ON TRIP TANK.
(M) (On) DRILL CEMENT AND FLOAT COLLAR FROM 14,906' TO 14,908' MONITOR ACTIVE SYSTEM FOR GAINS OR LOSSES. DRILLING PARAMETERS: PICK UP
692K SLACK OFF 662K, ROT 3 675K, ROP 0'-2', RPM 20-30, WOB 5K-20K, DRILLING PRESSURE 3,000 -3,500 PSI. MUD PUMP #2 AND #3 ON HOLE AT 61 SPM
EACH AT 650 GPM, MUD PUMP #4 ON BOOST AT 75 SPM AT 400 GPM.
DETAILS OF OPERATIONS IN SEQUENCE AND REMARKS
(M) (On) DRILL FLOAT COLLAR AND CEMENT FROM 14,908' TO 15,043'. BROKE THROUGH FLOAT COLLAR AT 14,911'. WASHED
DOWN
TO 14,948'. DRILL RATTY CEMENT FROM 14,948' TO 15,037'. DRILL FIRM CEMENT FROM 15,037' TO 15,043'. MONITOR ACTIVE FOR
GAINS OR LOSSES.
(M) (On) CIRCULATE BOTTOMS UP TO ABOVE TOP OF 11 7/8" LINER. MONITOR ACTIVE FOR GAINS OR LOSSES.
(M) (On) TAKE SLOW PUMP RATES AND CHOKE LINE FRICTION PRESSURES. CLOSE UPPER ANNULAR AND PERFORM D-5 DRILL
AS PER BP REQUIREMENT. MONITOR ACTIVE FOR GAINS OR LOSSES.
(M) (On) FLUSH CHOKE AND KILL LINES AFTER D-5 DRILL. MONITOR ACTIVE FOR GAINS OR LOSSES.CONDUCTED VISUALL
DERRICK INSPECTION.
(M) (On) DRILL CEMENT AND SHOE FROM 15,043' TO 15,103. DRILL CEMENT IN RAT HOLE FROM 15,103' TO 15,113'. MONITOR ACTIVE FOR GAINS OR
LOSSES. PARAMETERS AS FOLLOWS: WOB= 5-12K, RPM= 30-40, TORQUE= 7-14K, OFF BOTTOM TORQUE= 5-7K, PRESSURE 3400 PSI WITH PUMPS 2 & 4 AT
(M) (On) DRILL 10' GPM) PUMP #4 ON BOOST AT 75 SPM (400 GPM).
61 SPM EACH (645OF NEW HOLE FROM 15,113' TO 15,123', DRILLING PARAMETERS AS FOLLOWS: WOB 9-12, RPM= 40, TORQUE=8-11K, OB TORQUE= 5-
7K, PRESSURE 3400 PSI WITH PUMPS 2 &3 AT 61 SPM EA. (645 GPM), PUMP #4 ON BOOST AT 75 SPM (400 GPM) PICKUP= 706K, SLACK OFF= 673K,
ROTATING= 680K.
(M) (On) CIRCULATE CUTTINGS TO ABOVE TOP OF 11 7/8" LINER. PUMP UP STATIC DENSITY OF 13.6 PPG EMW. MONITOR ACTIVE
FOR GAINS OR LOSSES.
(M) (On) RACK BACK 1 STAND AND PICKUP TEST KELLY. PLACE BIT AT 15,079'. MONITOR WELL ON TRIP TANK.
(M) (On) HALIBURTON BROKE CIRCULATION DOWN KILL LINE AND CHICKSANS, TEST LINES TO 3000 PSI, GOOD TEST. PERFORM LEAK OFF TEST,
HALIBURTON PRESSURED UP TO 1020 PSI MAX PRESSURE. EQUIVALENT MUD WEIGHT OF 14.7 PPG. PUMP UP STATIC DENSI OF 14.786. MONITOR RISER
ON TRIP TANK. DOWN CHICKSAN LINES AND LAYDOWN TEST KELLY. TRIP IN HOLE FROM 15053' TO 15,123'. MONITOR WELL ON
(M) (On) RIG
TRIP TANK.
DETAILS OF OPERATIONS IN SEQUENCE AND REMARKS
(M) (On) CONTINUE DRILLING WITH 8 1/2" X 9 7/8" DRILLING ASSEMBLY FROM 17,634' TO 17,761'. DRILLING PARMETER ARE
AS FOLLOWS: WOB: 6/15 K, PUMP PRESSURE: 4,000 PSI , RPM : 120 , ROP: 60- 80' , P/U: 690 K , S/O : 660 K , ROT:
665 K , OB-TORQUE : 4/5 K PUMP #2 AND #3 ON HOLE @ 47 SPM ( 500 GPM.) PUMP #4 ON BOOST @ 70 SPM, ( 370 GPM.) MONITOR
ACTIVE SYSTEM FOR GAINS AND LOSSES. NOTED 134 BBL LOSS.
(M) (On) FLOW CHECK WELL UNABLE TO OBTAIN A NO FLOW . SHUT WELL IN @ 01:52, ON LOWER ANNULAR.
(M) (On) WELL SHUT IN AND MONITOR PSI OF 110 , WORK PIPE @ 02:47 HOURS PIPE FREE. BLEED PSI OFF TO MINI- TRIP
TANK @ 02:55 HOURS AND MONITOR FLOW BACK @ 18 BBLS PER HOUR. CLOSED BACK IN @ 3 BBLS BLEED BACK AND MONITOR PSI
OF 120 AFTER 7.5 MINUTES. BLEED PSI OFF @ 03:16 HOURS AND MONITOR FLOW BACK @ 24 BBLS PER HOUR. SHUT BACK IN
@ 03:24 HOURS AND MONITOR PSI. OF 140 AFTER 22 MINUTES, OPEN CHOKE @ 03:47 HOURS, BLEED PSI TO 0 PSI AND MONITOR
FLOW BACK @ 24 BBLS PER HOUR SHUT BACK IN @ 03:54 HOURS. MONITOR PSI OF 130 AFTER 8 MINUTES PSI DECREASED TO 120
PSI, AFTER 15 MINUTES, WORK PIPE @ 04:16 HOURS , ( PIPE FREE). BLEED PSI TO 0 PSI MONITOR FLOW BACK @ 24 BBLS
PER HOUR . SHUT IN @ 04-28 HOURS AND MONITOR PSI OF 120 AFTER 6 MNIUTES. OPEN @ 04:52 HOURS, BLEED TO 0 PSI FLOW
BACK @ 18 BBLS PER HOUR. SHUT IN @ 05:10 HOURS, MONITOR PSI OF 100 AFTER 6 MINUTES..OPEN CHOKE @ 05:30 HOURS BLEED
PSI TO 0 PSI AND FLOW BACK @ 12 BBLS PER HOUR, WORK PIPE @ 05:36 ( PIPE FREE). WORKED PIPE @ 0600 HOURS ( PIPE FREE),
@ 06:15 HOURS ( PIPE FREE). SHUT IN @ 06:25 HOURS MONITOR PSI OF 80 AFTER 20 MINUTES, @ 06:42 HOURS BLEED OFF.
@ 06:47 HOURS WORK PIPE ( PIPE FREE), @ 07:41 HOURS WORK PIPE ( PIPE FREE.)OPEN LOWER ANNULAR @ 08:23 HOURS. MONITOR
WELL ON TRIP TANK. TOTAL BBLS BLEED BACK: 34.8 BBLS. TOTAL BBLS LOST 24 HOURS 233 BBLS.
(M) (On) PUMP 184 BBLS , 84 POUNDS PER BBLS , LCM PILL SPOT @ 17,761' .MONITOR ACTIVE SYSTEM FOR GAINS AND LOSSES.
(M) (On) CONTINUE TO DRILL WITH 8 1/2" X 9 7/8" DRILLING ASSEMBLY FROM 17,761' TO 17,835'. DRILLING PARMETERS
ARE AS FOLLOWS: WOB: 11/12 K , PUMP PRESSURE : 3,990 PSI, RPM: 120 , ROP: 70' , P/U: 690 K, S/O: 660 K, ROT : 665
K , OB- TORQUE : 5/6 K , PUMP # 2 @ 75 SPM ( 400 GPM ). MONITOR WELL ON ACTIVE SYSTEM FOR GAINS AND LOSSES
(M) (On) WASH AND BACK REAM WITH 8 1/2" X 9 7/8" DRILLING ASSEMBLY FROM 17,835' TO 17,765'. LOG UP WITH SPERRY-SUN
DETAILS OF OPERATIONS IN SEQUENCE AND REMARKS
(M) (On) WASH DOWN FROM 17,745' TO 17,835' TAKE GEO-TAP AT BIT DEPTH 17,807' PROB DEPTH 17,723' = 14.15, BIT DEPTH
17,807 PROB DEPTH 17,722' = TIGHT, BIT DEPTH 17,809' PROB DEPTH =14.16, BIT DEPTH 17,808.5 PROB DEPTH 17,723.5 =
14.14 MONITOR ACTIVE SYSTEM FOR GAINS OR LOSSES.
(M) (On) CIRCULATE BOTTOMS UP AND CUT MUD # FROM 14.5 PPG TO 14.3 PPG MUD # AT 17,835'. PUMP 178 BBL LCM PILL.13:50
HOURS 14.3 PPG GOING IN HOLE.
(M) (On) PUMP OUT OF HOLE FROM 17,835' TO 17,634' MONITOR ACTIVE SYSTEM FOR GAINS OR LOSSES.
(M) (On) CONTINUE TO CIRCULATE BOTTOMS UP TO CUT MUD # FROM 14.5 PPG TO 14.3 PPG MUD #. MAX GAS 309 UNITS NO CUT
MUD. MONITOR ACTIVE SYSTEM FOR GAINS OR LOSSES.
(M) (On) FLOW CHECK AT 17,634'. FLOWED BACK 16 BBLS. IN 60 MIN. WELL STATIC.
(M) (On) FUNCTION TEST BOP'S FROM TOOL PUSHER'S CONTROL PANEL FROM YELLOW POD. FUNCTION DIVERTER AT 21:30 HRS FROM
TOOL PUSHER'S CONTROL PANEL ON YELLOW POD.
(M) (On) TAKE SCR'S AND WASH DOWN FROM 17,634' TO 17,835'. PUMP 100 BBL LCM PILL. MONITOR ACTIVE FOR GAINS OR LOSSES.
(M) (On) DRILL AHEAD FROM 17,835' TO 17,909' .DRILLING PARAMETERS : PICK UP 690K, SLACK OFF 655K, ROT# 680K, RPM
115, ROP 60'-80', WOB 10 - 15, MUD PUMP #3 ON HOLE AT 75 SPM AT 400 GPM AT 3150 PSI. MUD LOSS 0 BBLS
DETAILS OF OPERATIONS IN SEQUENCE AND REMARKS
(M) (On) CONTINUE TO WASH AND REAM WITH 8 1/2" DRILLING ASSEMBLY FROM 17,831' TO 18,234'. @ 18,193 FLOW RATE DROPS FROM 39% TO 29%.
PUMP PRESSURE REDUCED FROM 2,049 PSI TO 1,924 PSI . ECD DROP FROM 14.5 TO 14.4. DRILLING PARMETERS ARE AS FOLLOWS: WOB: -9.6, RPM: 25 ,
TORQUE: 5-6 K , P/U : 689 K ,S/O: 658, ECD: 14.48 , M.W. 14.0 PPG, PUMP PRESSURE: 1968 PSI, SPM: 57, GPM: 300. PUMP # 3 @ 57 SPM, MONITOR
ACTIVE SYSTEM FOR GAINS AND LOSSES.
(M) (On) WELL ON TRIP TANK @18,193' AND MONITOR 3.5 BBLS TO 2.4 BBLS PER HOUR TO 1 BBLS PER HOUR. MONITOR WELL
ON TRIP TANK FOR GAINS AND LOSSES.
(M) (On) PUMP 172 BBLS OF 84 LBS, 14.0 PPG LCM PILL @ 18,193' AND SPOT. MONITOR ACTIVE SYSTEM FOR GAINS AND
LOSSES.
(M) (On) CONTINUE TO WASH AND LOG WITH SPERRY-SUN WITH MWD AND 8 1/2" DRILLING ASSEMBLY FROM 18,234' TO 18,260'
MONITOR WELL ON ACTIVE SYSTEM FOR GAINS AND LOSSES.
(M) (On) CIRCULATE AND CONDITION MUD @ 18,260' SCR TAKEN @ 18,260' MAX GAS 479 UNITS. MONITOR ACTIVE SYSTEM
FOR GAINS AND LOSSES.
(M) (On) DRILL WITH 8 1/2" DRILLING ASSEMBLY FROM 18,260' TO 18,330' DRILLING PARAMETER ARE AS FOLLOWS: WOB: 4/8 K ,PUMP PRESSURE: 2,090
PSI , ROP: 25' , TOR : 10/ 12 K , P/U: 708 K , S/O: 677 K , ROT: 687 K , OB TOR: 5/7 K , PUMP # 3 ON HOLE @ 56 SPM (300 GPM)., PUMP # 4 ON BOOST@ 60
SPM ( 320 GPM). MONITOR ACTIVE SYSTEM FOR GAINS AND LOSSES.
DETAILS OF OPERATIONS IN SEQUENCE AND REMARKS
(M) (On) DRILL FROM 18,330' - 18,360' PUMP #3 DOWN HOLE AT 57 STROKES A MINUTE 300 GPM 1975 PSI. PUMP #4 ON RISER 60
STROKES A MINUTE 320 GPM. 700 PSI. PICK UP 708. SLACK OFF 677. DRILLING TORQUE 9- 12 K
(M) (On) CIRCULATE HOLE CLEAN AT 18,330' @ 300 GPM ON HOLE AND 320 GPM ON BOOST. TESTING CHOKE MANIFOLD TO 250
LO 6500 HIGH AND 5000 PSI ON BUFFER VALVES. 5 MIN. EACH TEST. PUMP UP STATIC DENSITY OF 14.22 PPG.
(M) (On) PUMPING OUT OF HOLE FROM 18,360' - 17,144' AT 300 GPM.TIGHT SPOT'S 18,195' 5 K OVER PULL 18,137' 10 K OVER PULL
18,132' 5 K OVER PULL.
(M) (On) FLOW CHECK MONITOR WELL ON TRIP TANK.
(M) (On) PICK UP TEST KELLY LOCATE ANNULAR RIG UP CHICKSAN LINE'S RIG UP TEST STUMP'S . BREAK CIRCULATION. TEST
LINE'S TO 7,500 PSI.
(M) (On) TEST BOP ON 6 5/8" DRILL PIPE AS PER MMS AND BP REQUIREMENTS. TEST PERFORMED FROM DRILLERS PANEL ON
BLUE POD. 250 PSI LOW 3,500 PSI HIGH. 5 MIN EACH TEST. TEST LOWER ANNULAR AND ASSOCIATED VALVES.
DETAILS OF OPERATIONS IN SEQUENCE AND REMARKS
(M) (On) CONITNUE SUB-SEA BOP TEST AS PER BP AND MMS REQUIREMENTS, ON 6 5/8 DRILL PIPE. TEST PERFORMED FROM
DRILLERS
PANEL ON BLUE POD . TEST LOWER ANNULAR AND ASSOCIATED VALVES TO 250 PSI LOW AND 3,500 PSI HIGH FOR 5 - MINUTES
EACH TEST STAIGHT LINE TEST. UPPER ANNULAR, KELLY HOSE, AND ASSOCIATED TO 250 PSI LOW 5-MINUTES STRAIGHT LINE
AND
5,000 PSI HIGH UNITL GREEN LIGHT ON ANATOMIZED DIGITAL BOP TESTING. TEST ALL PIPE RAMS AND FAIL SAFE TO 250 PSI
LOW FOR 5 - MINUTES STAIGHT LINE AND 6,500 PSI HIGH UNTIL GREEN LIGHT ON ANATOMIZED DIGTIAL BOP TESTING. SEE
TEST
CHART, FOR ADDITIONAL INFORMATION. MONITOR BOP PRESSURE AND TRIP TANK WELL STATIC.
(M) (On) RIG DOWN HALLIBURTION CHICKSAN LINES AND LAY OUT TEST KELLY @ 17,006'. MONITOR WELL ON TRIP TANK WELL
STATIC.
(M) (On) PULL OUT OF THE HOLE WITH 8 1/2" DRILLING ASSEMBLY FROM 17,006 TO 16,667'. ( NOTED FROM 17,006' TO 16,914'
18-30 K DRAG ) ( 16,672' TO 16,667' 10-15 K DRAG) SLACK OFF FROM 16,667' TO 16,693. MONITOR WELL ON TRIP TANK FOR
GAINS AND LOSSES.
(M) (On) MAKE -UP TOP DRIVE CIRCULATE FOR 15 MNIUTES PER BP WORK PIPE UP TO 16,594' AND DOWN TO 16,731'. NO DRAG
NOTED. LOCATE ON UPPER ANNULAR TO SPACE OUT TO TEST.MONITOR WELL ON ACTIVE SYSTEM FOR GAINS AND LOSSES.
(M) (On) CONITNUE SUB-SEA BOP TEST AS PER BP AND MMS REQUIRMENTS, ON 5 1/2" DRILL PIPE. TEST PERFORMED FROM DRILLERS
PANEL ON BLUE POD . TEST LOWER ANNULAR AND ASSOCIATED VALVES TO 250 PSI LOW AND 3,500 PSI HIGH FOR 5 - MINUTES
EACH TEST STAIGHT LINE TEST. AND 3,500 PSI HIGH GREEN LIGHT ON ANATOMIZED DIGITAL.TEST UPPER ANNULAR AND ASSOCIATED
VALVES 250 PSI LOW 5- MINUTE STRAIGHT LINE AND 3,500 PSI UNTIL ANATOMIZED GREEN LIGHT. TEST ALL PIPE RAMS AND FAIL
SAFE TO 250 PSI LOW FOR 5 - MINUTES STAIGHT LINE AND 6,500 PSI HIGH UNTIL GREEN LIGHT ON ANATOMIZED DIGTIAL BOP
TESTING. SEE TEST CHART, FOR ADDITIONAL INFORMATION. MONITOR BOP PRESSURE AND TRIP TANK WELL STATIC.
(M) (On) PERFORM FUNCTION TEST AS PER BP AND MMS REQUIRMENTS FROM TOOLP USHER PANEL ON YELLOW POD,@ 16,663'. FUN
TEST, DIVITER FROM TOOL PUSHER PANEL ON YELLOW POD @ 0838 HOURS. MONITOR WELL ON TRIP TANK WELL STATIC.
(M) (On) PUMP OUT HOLE FROM 16,693' TO 15,493' PUMP #3 @56 SPM ( 300 GPM ).MONITOR ACTIVE SYSTEM FOR GAINS AND LOSSES.
DETAILS OF OPERATIONS IN SEQUENCE AND REMARKS
(M) (On) PUMP OUT OF HOLE FROM 15,493' TO 14,667'. PULL OUT WET TO 14,117'. PUMP PRESSURE 1700 PSI. 57 STROKES A MINUTE 300 GPM.
(M) (On) PUMP 75 BBL'S 17 PPG SLUG.
(M) (On) PULL OUT OF HOLE FROM 14,117' TO 1,155'. MONITOR PIPE DISPLACEMENT ON TRIP TANK.
(M) (On) PULL OUT OF HOLE WITH HEAVY WEIGHT DRILL PIPE AND DRILL COLLAR'S FROM 1,155' TO 73'. MONITOR PIPE DISPLACEMENT ON TRI
(M) (On) LAY OUT BHA ON RISER SKATE FROM 73' TO SURFACE.
(M) (On) CLEAN AND CLEAR RIG FLOOR OF BHA HANDLING EQUIPMENT.
(M) (On) HELD PRE-JOB MEETING ON RIGGING UP WIRE LINE EQUIPMENT AND PICKING UP TRIPLE COMBO WIRE LINE TOOL'S.
(M) (On) RIG UP WIRE LINE EQUIPMENT
(M) (On) LOAD RADIO ACTIVE SOURCE TEST TRIPLE COMBO WIRE LINE TOOLS.
DETAILS OF OPERATIONS IN SEQUENCE AND REMARKS
(M) (On) HELD PRE-JOB SAFETY MEETING WITH CREW ON PULLING OUT OF THE HOLE. MONITOR WELL ON TRIP TANK, WELL
STATIC.
(M) (On) PULL OUT OF THE HOLE WET FROM 14,759' TO 14,020'. MONITOR PIPE DISPLACEMENT ON TRIP TANK.
(M) (On) FUNCTION TEST SUBSEA BOP'S AS PER BP AND MMS REQUIRMENTS ON BLUE POD FROM DRILLERS CONTROL PANEL.
FUNCTI DIVERTER AT 01:25 HRS FROM DRILLERS CONTROL PANEL ON BLUE POD. MONITOR WELL ON TRIP TANK, WELL STATIC.
(M) (On) PUMP 70 BBLS OF 16.8 PPG SLUG. MONITOR ACTIVE SYSTEM FOR GAINS AND LOSSES.
(M) (On) PULL OUT OF THE HOLE FROM 14,020' TO 6,725'. MONITOR PIPE DISPLACEMENT ON TRIP TANK. PULLED WEAR BUSHING
WITH 120K OVERPULL.
(M) (On) PERFORM 5 MINUTE FLOW CHECK PRIOR TO LAYING DOWN DRIL-QUIP WEAR BUSHING RETRIEVAL TOOL FROM 6,725'
TO 6,664' NO WEAR BUSHING RECOVERED. MONITOR PIPE DISPLACEMENT ON TRIP TANK. NO WEAR BUSHING RECOVERED.
MONITOR PIPE DISPLACEMENT ON TRIP TANK.
(M) (On) PULL OUT OF THE HOLE FROM 6,664' TO 1,155'. MONITOR PIPE DISPLACEMENT ON TRIP TANK.
(M) (On) PULL OUT OF THE HOLE WITH 5 1/2" HEAVY WEIGHT DRILL PIPE FROM 1,155' TO 262'. MONITOR PIPE DISPLACEMENT ON
TRIP TANK.
(M) (On) HELD PRE-JOB SAFETY MEETING WITH CREW ON LAYING DOWN BHA. MONITOR WELL ON TRIP TANK, WELL STATIC.
(M) (On) LAY DOWN BHA FROM 262' TO SURFACE. MONITOR PIPE DISPLACEMENT ON TRIP TANK.
(M) (On) CLEAN AND CLEAR RIG FLOOR. MONITOR WELL ON TRIP TANK, WELL STATIC.
(M) (On) PICK UP DRIL-QUIP WASH SUB FROM SURFACE TO 51'. MONITOR DIAPLACEMENT ON TRIP TANK.
DETAILS OF OPERATIONS IN SEQUENCE AND REMARKS
(M) (On) HOLD PRE-TASK SAFETY MEETING ON PICKING-UP DRIL-QUIP MULTI-PURPOSE TOOL. MONITOR WELL ON TRIP TANK
WELL STATIC.
(M) (On) RUN IN HOLE WITH 6 5/8" TAIL PIPE FROM 51' TO 1,152'. MONITOR PIPE DISPLACEMENT ON TRIP TANK.
(M) (On) PICK-UP DRIL-QUIP MULTI-PURPOSE TOOL ASSEMBLY FROM 1,152' TO 1,222'. MNOITOR PIPE DISPLACEMENT ON TRIP
TANK.
(M) (On) CONTINUE TO RUN IN HOLE WITH DRIL-QUIP MULTI-PURPOSE TOOL ASSEMBLY FROM 1,222' TO 5,004' @ 2 MINUTES
PER STAND. MONITOR PIPE DISPLACEMENT ON TRIP TANK .
(M) (On) WASH BOP STACK AND WELL HEAD FROM 5,004' TO 5,088' @ 10 BBLS PER MINUTE AND BOOST RISER @ 10 BBLS PER
MNIUTE. MONITOR ACTIVE SYSTEM FOR GAINS AND LOSSES.
(M) (On) CONITNUE TO RUN IN HOLE WITH DRIL-QUIP MULTI-PURPOSE TOOL ASSEMBLY FROM 5,088' TO 6,170'. MONITOR PIPE
DISPLACEMENT ON TRIP TANK.
(M) (On) CONTINUE TO RUN IN HOLE WITH DRIL-QUIP MULTI-PURPOSE TOOL FROM 6,170' TO 6,229'. STAGE BOOST PUMP UP TO 10 BBLS PER MNIUTE. @
5,060' LATCH INTO WEAR SLEEVE SLACK-OFF TO 30 K DOWN, PICK-UP TO 80 K OVER PULL, SLACK-OFF TO NETURAL, PICK-UP 105 K OVER PULL, SLACK-OFF
TO NETURAL, PICK-UP 135 K OVER PULL, SLACK-OFF TO NETURAL, PICK-UP 160 K OVER PULL AND WEAR SLEEVE CAME FREE. PICK-UP WITH INCREASE OF
17 K ON HOOK LOAD. SAW 200 PSI INCREASE WHEN PULLING BY BOOST PRESSURE. CONTINUE TO PICK-UP TO 6,170'. MONITOR ACTIVE SYSTEM FOR
GAINS AND LOSSES. OF HOLE WITH DRIL-QUIP MULTI-PURPOSE TOOL ASSEMBLY FROM 6,170' TO 5,088'. MONITOR PIPE
(M) (On) PULL OUT
DISPLACEMENT ON TRIP TANK. WELL ON ACTIVE SYSTEM FOR GAINS AND LOSSES.
(M) (On) WASH WELL HEAD FROM 5,088' TO 4,954' @ 10 BBLS PER MNIUTE. PUMP 30 BBL 16.7 PPG SLUG @ 4,954' MONITOR
(M) (On) CONTINUE TO PULL OUT OF HOLE WITH DRIL-QUIP MULTI-PURPOSE TOOL ASSEMBLY. FROM 4,954' TO 1,222'. DROP 2
5/8" DRIFT @ 4,954'. MONITOR PIPE DISPLACEMENT ON TRIP TANK .
(M) (On) PULL AND LAY DOWN DRIL-QUIP WEAR SLEEVE. FROM 1,222' TO 1,152' REMOVED WEAR SLEEVE FROM MULTI-
PURPOSE TOOL. MONITOR WELL ON TRIP TANK WELL STATIC.
(M) (On) CONTINUE TO PULL OUT OF HOLE WITH TAIL PIPE FROM 1,152' TO 51'. PERFORM FUNCTION TEST ON BLIND SHEAR
RAMS FROM TOOL PUSHER PANEL ON YELLOW POD @ 23:00 HOURS. MONITOR PIPE DISPLACEMENT ON TRIP TANK.
(M) (On) PULL AND LAY DOWN DRIL-QUIP WASH SUB ASSEMBLY FROM 51' TO SURFACE. MONITOR PIPE DISPLACEMENT ON
TRIP TANK
(M) (On) CLEAN AND CLEAR RIG FLOOR . MONITOR WELL ON TRIP TANK WELL STATIC.
DETAILS OF OPERATIONS IN SEQUENCE AND REMARKS
(M) (On) CONTINUE DISPLACING CEMENT WITH 727 BBLS OF 14.0 PPG MUD. WITH 4,155 STKS/ 523 BBLS PUMPED TOP PLUG WENT
THROUGH X-O WITH 590 PSI. BOTTOM PLUG LANDED WITH 673 BBLS PUMPED AT 2,932 PSI. WITH 727 BBLS PUMPED, BUMPED TOP
PLUG WITH 740 PSI OVER CIRCULATING PRESSURE. BLED PRESSURE OFF, BLED BACK 5 BBLS, FLOATS HOLDING. CEMENT IN PLACE
AT 12:35 HRS.
(M) (On) RELEASE DRIL-QUIP RUNNING TOOL AND SET SEAL ASSEMBLY AT 5,059'. SLACK OFF TO 350K HOOKLOAD, MAKE 6 TURNS
TO RIGHT. SET SEAL ASSEMBLY WITH 320K HOOKLOAD. MONITOR WELL ON TRIP TANK, WELL STATIC.
(M) (On) BREAK CIRCULATION DOWN KILL LINE. HALLIBURTON TEST LINES TO 11,000 PSI, GOOD TEST. CLOSED UPPER PIPE RAMS,
HALLIBURITON PRESSURE TEST SEAL ASSEMBLY TO 4,000 PSI HOLD FOR 30 SEC. PRESSURE UP TO 10,000 PSI HOLD FOR 10 SEC.
BLED PRESSURE OFF TO 6,500 PSI HOLD FOR 5 MINUTES.
(M) (On) SHEAR OUT OF SEAL ASSEMBLY WITH 85 K OVER STRING WEIGHT. CIRCULATE 10 MINUTES TO FLUSH OUT HANGER. MONITOR
ACTIVE SYSTEM FOR GAINS AND LOSSES.
(M) (On) SLACK OFF TO 335 HOOKLOAD, CLOSE UPPER PIPE RAMS. HALLIBURITON PRESSURE UP ON SEAL ASSEMBLY TO 10,000 PSI
FOR 10 SEC. BLED OFF TO 6,500 PSI, HOLD FOR 5 MINUTES.
(M) (On) RIG DOWN CHIKSAN LINES AND LAY DOWN CEMENT KELLY. MONIOTR WELL ON TRIP TANK, WELL STATIC.
(M) (On) PULL OUT OF THE HOLE WET FROM 5,059' TO 4,770'. MONITOR DISPLACEMENT ON TRIP TANK.
(M) (On) DROP FOAM WIPER BALL AND CIRCULATE 1 1/2" TIMES THE DRILL PIPE VOLUME. PUMPED 30 BBLS OF 16.3 PPG SLUG.
MONITOR ACTIVE SYSTEM FOR GAINS AND LOSSES.
(M) (On) PULL OUT OF THE HOLE WITH LANDING STRING FROM 4,770' TO 51'. MONITOR DISPLACEMENT ON TRIP TANK.
(M) (On) LAY DOWN DRIL-QUIP RUNNING TOOL FROM 51' TO SURFACE. MONITOR DISPLACEMENT ON TRIP TANK.
(M) (On) CLEAN AND CLEAR RIG FLOOR. MONITOR WELL ON TRIP TANK, WELL STATIC.
(M) (On) HELD PRE-JOB MEETING WITH CREW ON RIGGING UP AND RUNNING 3 1/2" TUBING. MONITOR WELL ON TRIP TANK, WELL STATIC.
DETAILS OF OPERATIONS IN SEQUENCE AND REMARKS
(M) (On) HELD PRE-TASK MEETING ON RUNNING IN HOLE WITH DRILL PIPE. MONITOR WELL ON TRIP TANK WELL STATIC.
(M) (On) CONITNUE TO RUN IN HOLE WITH 3 1/2" TUBING FROM 4,817' TO 8,367'. MONITOR PIPE DISPLACEMNT ON TRIP TANK.
(M) (On) PICK-UP TEST KELLY AND RIG UP CHICKSAN LINES @ 8,367' MONITOR WELL ON TRIP TANK WELL STATIC.
(M) (On) HALLIBURTON BREAK CIRCULATION AND TEST LINES TO 3,000 PSI. ( GOOD TEST). MONITOR WELL ON TRIP TANK WELL STATIC.
(M) (On) HOLD PRE-TASK MEETING ON DISPLACE BOOST, CHOKE AND KILL @ 8,367'. MONITOR WELL ON TRIP TANK WELL STATIC.
M.) MONITOR
AND MONITOR PSI
AND MONITOR
REASED TO 120
TO 0 PSI FLOW
0 HOURS BLEED
RS ( PIPE FREE),
3 HOURS. MONITOR
AND LOSSES.
AT 21:30 HRS FROM
NS OR LOSSES.
ED FROM DRILLERS
R AND ASSOCIATED
AMS AND FAIL
POD,@ 16,663'. FUN
NS AND LOSSES.
OKES A MINUTE 300 GPM.
PE DISPLACEMENT ON TRIP TANK.
P PLUG WENT
, BUMPED TOP
CEMENT IN PLACE
MAKE 6 TURNS
ER PIPE RAMS,
D FOR 10 SEC.
HANGER. MONITOR
LY TO 10,000 PSI
P TANK, WELL STATIC.
TANK WELL STATIC.
WELL STATIC.
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