Cleaning Schedule Templates - PowerPoint

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Cleaning Schedule Templates document sample

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scope of work template
							 P ractical          Case                                                                                 Kaizen Dates: Jan 16 – Jan 20
Process
Improvement          Study
                                                    Objective: Cell           Design
          The goal of the Kaizen team was to design and develop an integrated printer repair business that would eliminate
        cumbersome equipment; reduce wait time in between operations; reduce distance traveled by both cell operators and
       equipment to improve output and cycle time; and optimize the placement and replenishment of parts needed in the cell
                                                      to decrease inventory.


                                                        Kaizen Targets:

                                           • Eliminate off-line cleaning
                                           • Eliminate NVA walking, waiting                                                  To shipping
                                           • Reduce distance the product travels
                                           • Place parts and incoming units at the line,
                                                supported by replenishment
                                                                                                          Inbound


                                                             Kaizen Success:

                                                                   Before Kaizen After Kaizen % Change
                                         Inventory (units)              105          50         47%

                                       Avg cycle time (minutes)          46         34.50       25%

                                        Output per employee              12         19-26      58- 100%


                                                         What the customer did:

      The process was laid out in a functional manner that caused batching at 4 different steps in the process. The team identified
  significant non-value added time in the form of walking, movement, handling and waiting. This NVA was reduced or eliminated by
          using a cell design that features consistent material availability and single-piece flow on a continuous work surface.
  P ractical                                                                                           Kaizen Dates: Nov. 15 – Nov. 19
 Process               Case
 Improvement           Study
                                     Objective: Total             Productive Maintenance
        The purpose of this Kaizen Blitz is to improve the ability to respond to customer’s demand through improved asset
        utilization, workplace organization and visual management.




                                                         Kaizen Targets:
                                     • Complete Phase 1 & 2 TPM improvement activity
                                     • Improve OEE by 25% with 2 months
                                     • Improve Workplace Organization and Visual Management


                                                           Kaizen Success:

                                                                       Before Kaizen After Kaizen % Change
       Leaking Seal                     Overall Equip. Effectiveness       49%         69%          20%             Repaired Seal
                                           Scrap reduction                $5400        $120         99%

                                           5s rating (out of 5)            1.32        3.4          160%


                                                       What the customer did:
The team spent two intense days of training on TPM concepts and identifying opportunities for improvement on the shop floor. The
next three days’ efforts included cleaning, sorting, inspection, machine modifications and/or laying out work areas for better
maintenance work flow. The team also did calibration, data collection, & lubrication on the equipment, as well as addressing safety
issues that will ensure sustainable OEE.
 P ractical                                                                                    Kaizen Dates: June 27 – July 1
Process             Case
Improvement         Study
                                              Objective: Set-up           Reduction
     The purpose of this Kaizen is to reduce Set-up time by 55%, reduce the complexity (“Black Art”) of the changeover
     process, and ensure participation & ownership by all team members to sustain the changes.




                                                   Kaizen Targets:
                                • Reduce changeover time on the 200 Ton Press by 55%
                                • Improve Productivity by 25% with 2 months
                                • Improve Workplace Organization and Visual Management


                                                      Kaizen Success:

   Multi-piece clamp
                                                               Before Kaizen After Kaizen % Change        One-piece clamp
                                        Time (minutes)               60          12         80%

                                    Operator movement (feet)       2122         450         79%

                                    Number of work elements          46         29          34%


                                                 What the customer did:
  The team correctly identified 47 minutes (out of 60) of non-value added time in the form of waiting, searching, and adjustment
  (clamps, dies, positioning). The internal/external activities were identified, corrective actions were suggested and tested via
  “try-storming” efforts, adapted as required, and implemented for immediate use. Solutions included line-side storage of dies,
  one-piece clamps, standard die heights, and common die positions in the press. Training of the remaining operators occurred and
  Standard Work provided the documentation required to sustain the changes.
   P ractical                                                                                             Kaizen Dates: 3/20 – 3-24
  Process                Case
  Improvement            Study

                                Objective: Strategic Value                    Stream Mapping (VSM)
          The purpose of this Kaizen is to identify a strategy, execution tools and targeted areas that will allow us to reach
          Customer Satisfaction, On-time delivery and growth objectives in our current fiscal year.

                                                               Kaizen Targets:
                                                    • Reduce Process Lead time by 60%
                                                    • Identify specific actions to implement
                                                    • Train the leadership team in the VSM tool.
                                                    • Redesign Demand Management process

                                                                   Kaizen Success:
                                                                           Before Kaizen After Kaizen % Change
                                            Process Lead time (days)             21        10.7         50%

                                           Specific action items                  0         56         XX%

                                          Leadership team trained in VSM          2         16         XX%
       Current State VSM                                                                                              Future State VSM

                                                       What the customer did:
Key observations of the current state:                                                        Recommended focus on key areas:
-    Forecast demand changes within process lead-times
                                                                                              - Demand management process re-design
-    Excessive/redundant Test time
-    Excessive movement of parts                                                              - Process improvements in Head, Reservoir, Curing, Test
-    Excessive variety of fasteners                                                           - Process Improvements in Final Assy.
-    Parts availability
-    Excessive pick time of parts for subs (50% of cycle time)
-    High frustration level due to parts shorts, overtime, schedule changes
-    Outdated/inefficient design solutions
    P ractical        Case                                                    Date: Oct. 28 th – Dec. 15th 2008
   Process                               Hi-Volume Cell
   Improvement
                      Study
                                                                        Targets: (Press Brake to Paint)
                                                                        1. Increase productivity by 25%
                                                                    2. Achieve On-time delivery goal of 95%
                                                             Metrics          Beginning      Goal    Comments           1/7/09
 Design Team: Marty Bogue, Don Masters (Leader), Brian
 Nichols, Rob Carlson, Rob Marelli, Howie Bogue,                                State                                     Status
                                                                              (10/28/08)
 Trial-Team: Sindy Lighthouse; Mike Fortunado; Carlus    Process Lead         5 days         1 day      Focus on         8.3 hours
 Davis; John Aledia; John Berg                                                                           distance
                                                         time (250 pc lot)
                                                                                                     travelled and 1-
                                                                                                        piece flow

                                                         Distance travelled
                                                                               502 ft      250 ft      Reduce total      200 ft
                                                                                                     by 50%




The Design Team reviewed the
current layout and quickly observed
a number of problems such as
large batches, long wait times, and
excessive material movement. The
major focus is on the reduction of
travel distance, efficiency of the
operator, elimination of wait time.
The Trial Team ran the first
production to achieve 50%
reduction in process time.
 P ractical                                                                     Date: Dec. 13thth – Dec. 15th 2008
Process              Case
Improvement          Study
                                                                                               Targets:
                                                              1. Increase 6S score by 33% and sustain the changes


                                                                    Metrics       Beginning     Goal      Comments        1/09/09
                                                                                    State                                   Status
                                                                                  (12/13/08)

                                                                 Increase 6S      45 (out of     60       Audit planned       61
                                                                 score by 33%     99)                      for week of
Brian Nichols, Jason Scott, Jeff Reinhart, Casey                                                              1/5/09
Harrington, Lisa Robison

   6S Punch Press
                                        A Seconn team conducted a 6S effort on the
                                        Punch Press. Activities included: SORT:
                                        Remove all unneeded objects; STABILIZE:
                                        Organize all tools and work spaces; SHINE:
                                        Clean/Sweep all areas in/under/around the
           Before                       machine; STANDARDIZE: Tape floors, mark                             After
                                        tool locations, display procedures; SUSTAIN:
                                        Make sure everybody sticks to the rules.
                                        SAFETY: Provide a safe and healthy
                                        workplace
Account Payable Process

     Acme Corporation                                              Date: May 14 – May 15

                                                  Targets:
                                                  • Reduce Process Leadtime by 50%
                                                  • Identify and recommend changes to implement




                                                                                                          %
                                                        Metric             Before           After         Improve

                                                Leadtime
                                                                         7.2 hours      3.16 hours         57%




The team looked at the details that made
up the current process and quickly
observed a number of problems such as
labor inefficiencies, excessive wait time,
and lack of standard work. The team has
identified and prioritized 12 action items
to address the problems. The major
                                                 7.2 hours
focus is on the elimination of wait time,                                                    3.6 hours
and process changes to eliminate             Current State                                 Future State
redundant process time.
         P ractical                                                                                                                                                                                                                                       Kaizen Dates: 4/26 – 4/28
        Process                                                                                       Case
        Improvement                                                                                   Study
                                                                             Objective: Office Kaizen-New                                                                                                  Product Manufacturability Process Reduction
                                                                 The purpose of this Kaizen is to review all activities related to the basic manufacturability analysis process including
                                                                 data preparation, policies and practices, and DFx Guide. The team will identify and recommend changes (short/long
                                                                 term) that will significantly reduce the process time, simply the process, and reduce redundancy in the process.


                                                                                                                                                                                                                Kaizen Targets:
                                                                                                                                                                                   • Reduce customer notification to deliver DFM report time by 50%
                                                                                                                                                                                   • Reduce number of report generation steps by 25%
                                                       Current State Map – DFM Process                                                                                                                                                                                                                      Future State Map – DFM Process
              Customer
                                                                                                                                                                                                                  Kaizen Success:
                                                                                                                                                                                                                                                                                                                                                                                                            Customer
     Resource & Data
                                                 Matrix Data Rework     ODB++ Rework
                                                                                                                 Analysis Rework
                                                                                                                                                                                                                  Before Kaizen   After Kaizen % Change      Receive Notification
                                                                                                                                                                                                                                                                (from CAD PDM)
                                                                                                                       5%
Notify & Assign   Data There?                           20%                 10%
   7 inputs
   3 steps
                  5 scenarios
                    2 steps                                                                                       Process Map
                                                                                                                                                                                              Number of steps           51            12        77%
       1               1                                                                                            Rework
                                                                                                                       5%


  7.4 hour        4.4 hour
                                NVA                                                                                                                                                           Lead time (hours)         32          12.3        62%
                             11.8 hrs




                                                                                                                                                                                                                                                                             Launch Valor &   Automated Attr.   Manual Attr. Ass’t   Review Results   Manual Analysis   Create Report   Add Rec’ations to    Publish to web
                                Data Prep & VWR         Data Handling         Job Prep          Verify Results        Export Report   Manual Checks         Report Generation                                                                                                  Open Job        Assignment        & Run Analysis                                                              Report          portal & notify

                                       9 steps                4 steps          19 steps            5 steps               3 steps         4 steps                 7 steps          Customer
                                        1

                                                                                                                                                                                     TLT                                                                                            1                                                                                                                                            TLT
                                                                                                                                                                                    32 hrs                                                                                                                                                                                                                                     12.3 hrs
                                      5.2 hour            2.6 hour        3.5 hour               6.4 hour               0.2 hour      0.1 hour              8.5 hour                                                                                             4 hours       5 minutes                                             180 minutes                        10 minutes                             10 minutes
                                                                                                                                                                                      VA                                                                                                       20 minutes         36 minutes                                                                                                    60 %
                                                                                     0.8 hour                                                      4 hour              0.8 hour                                                                                                                                                                        180 minutes                        60 minutes                             VA
                                                                                                                                                                                    5.6 hrs
                                                                                                                                                                                     17 %                                                                                                                                                                                                                                        296
                                                                                                                                                                                                                                                                                                                                                                                                                                40 %




                                                                                                                                                                                                    What the customer did:
                       The Design for Manufacturability process was identified as a strategic process to drive profit planned margins for new products.
                       The lead-time, based on the current state map, was 32 hours to interpret customer requirements and confirm that the product can
                       be manufactured as designed. The team looked at each of the steps in the process and identified significant waste in the form of
                       wait time and redundant manual verification of data. Steps were eliminated, sequences were changed, and software changes
                       were made to use exception reporting to highlight manufacturability issues.

						
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